Well, I've been busy. Thanks to Craig Cheetham, the car is now back in one piece and relatively straight.
IMG_20180928_122620297 by
max_burton, on Flickr
After the trip down to the Fens however, the car started to condense its header tank It was misfiring, a little down on power and hunting in neutral.
Fearing the worst, and considering the cambelt was due on age, supposedly last having been done at around 50k in 2003, I figured it was worth going whole hog. Everything to recondition the head was ordered, and over the last week or so my dad and I have been working on it all.
We were right to fear the worst.
The stainless 4-2-1 manifold has also been fitted, and the original exhaust bodged back on until the car is booked in for a stainless system.
To compliment this I also ordered a washable K&N air filter element - I ordered it from Amazon from a company in Croatia, as it was by far the cheapest one available. Only one was in stock.
To my surprise the part turned out to be NOS, dated 1997!
The car is all back together now, ready for a shakedown this evening. There's a bit of vibration (I had to use standard bolts in place of compensators to join the exhaust together as the Japspeed stainless downpipe is 2" shorter than the original one, think it's off a Civic) but it's running well. The improvement in performance is subtle, but suits the car well. It's smooth and refined, and goes a lot faster than it feels like it is. Wonderfully relaxed.
